The truck is a "spare" that I don't use very often. This year I've already put a clutch and a new AC compressor/hoses and a water pump. Feelin tired of spending money and time on it. The truck was running OK. If it runs a little better with more compression I'll consider that a bonus!
Hopefully I got rid of the air bubbles in the coolant issue.
Might look at a rebuild in a few years, when I retire and can take my time.
Anyway, the thing with the valves is kind of an experiment.
I'll learn from it. If it work out well, I know I can remachine valves, and if it fails, I'll know it's a bad idea!
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Quote:
Originally Posted by tomboy
How thin were the edge of the valves after you cut them, there's a limit, and what about the seats, they need to be ground and trued up also.
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I didn't measure the edges but it didn't change very much. I think they still look good.
The seats didn't look like the valves. They looked surprisingly good.
I lapped until I had solid grey all the way around and uniform thickness.
Crossing my fingers but it's going back together.
I'll let ya'll know how it goes...
:-)