High RPM misfire
Hi, my younger brother owns a 98 ranger with the Vulcan 3.0L in it, and we have hit a dead end trying to solve a misfire problem. This truck has just over 150,000 miles on it, and runs excellent 99% of the time, it isn't until the engine is pushed to high RPM that the misfire occurs (we're not taking it to the rev-limiter, we've never run it that hard). The truck won't throw a code, and we have no idea what the cause of the miss could be.
Here's the deal: When driving the truck it will not miss at all unless the engine is pushed to 3000 RPM. When it hits 3000 RPM EXACTLY, there is a very noticeable stutter in the engine and it takes a very long time for it to reach 3500 RPM under this condition. It makes it hard to drive because he needs to shift at a higher RPM when pulling out into traffic or going uphill. Anything that drops RPM (shifting/letting off throttle) clears this up, but it will misfire every time its is pushed to 3000 RPM. My brother also tells me that it runs worse in the morning when its cold outside. We have tried everything and have come no closer to solving this issue, so I'm hoping that somebody out there knows more about this particular problem than we do.
What we've done to fix this: (These have all been replaced within the last three years)
-New Plugs (less than a week old)
-New Plug Wires (less than a week old)
-New Throttle Positioning sensor
-New Idle Air Control Valve
-New EGR Valve
-New Synchronizer and Camshaft position sensor (the synchronizer is not loose, it was the first thing we checked)
-Mass Air Flow sensor was cleaned
-Numerous vacuum leaks were corrected via smoke test
-Coil pack is in good shape
As a last result we took this truck to a mechanic who put it on a dyno with the engine hooked up to a diagnostic machine. He found that the engine was suffering from constant lean misfires, and discovered that the rubber intake tube from the airbox to the upper intake manifold was cracked 2/3 of the way around the diameter, and was letting an excessive amount of air into the intake manifold. He replaced this intake tube and the misfire cleared up for two days and came back. It isn't as severe as it was before, but it still affects the truck's drivability.
Last edited by 98.3.0.ranger; 05-31-2019 at 08:04 AM.
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